new to me boat. 2006 df 115 tk5
my brother and i went in on the boat 1/2-1/2. 2006 carolina skiff 2180.
he brought it back and i went and picked it up. left key on trailer and lost the key.
i took apart the remote throttle controls to access the back of the ignition switch to order a new key.
had a hell of a time getting it all back together. i also located the key later that night.
at that junction, i had only turned over and heard the motor run 5 min on muffs. my brother picked it up out of area.
after my messing w throttle control and installing vhf radio, it fired up like normal, quick and snappy. idled for about 5 minutes on muffs beautifully then sounded like it was out of gas. would not restart.
injnow there's gas in it. after 20 min i go to restart and i get the 4-2 code, cam/crank sensor. give it a couple hours, do the reset (key in on position, pull kill switch lanyard and pull the switch 2 more times in 10 sec). it reset, it started beautifully, idled on muffs again and at about 600 rpm. sounded smooth. idled up, idled down, put it in gear, beautiful. 5 -10 min later, just sounded like it ran out of gas.
aftaid to continue messing w it unless i know what to do. the motor head in me says, it sat for a couple weeks and just needs to be run
my brother and i went in on the boat 1/2-1/2. 2006 carolina skiff 2180.
he brought it back and i went and picked it up. left key on trailer and lost the key.
i took apart the remote throttle controls to access the back of the ignition switch to order a new key.
had a hell of a time getting it all back together. i also located the key later that night.
at that junction, i had only turned over and heard the motor run 5 min on muffs. my brother picked it up out of area.
after my messing w throttle control and installing vhf radio, it fired up like normal, quick and snappy. idled for about 5 minutes on muffs beautifully then sounded like it was out of gas. would not restart.
injnow there's gas in it. after 20 min i go to restart and i get the 4-2 code, cam/crank sensor. give it a couple hours, do the reset (key in on position, pull kill switch lanyard and pull the switch 2 more times in 10 sec). it reset, it started beautifully, idled on muffs again and at about 600 rpm. sounded smooth. idled up, idled down, put it in gear, beautiful. 5 -10 min later, just sounded like it ran out of gas.
aftaid to continue messing w it unless i know what to do. the motor head in me says, it sat for a couple weeks and just needs to be run
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