Hoping all of you can help me. I have learned a ton from this site and had troubles getting registered but finally got approved to make a posting here! You folks are awesome at helping the users out. Thanks in advance!!
My father in law has a low hour 2005 Suzuki 50hp four stroke mated to a Carolina Skiff. The motor has been a flawless runner. Always started, idled like a dream, ran out at higher rpms with no issues, sipped gas, very fun to run and very quiet for trolling. This boat was used only a few times every summer in freshwater lakes in MI and stored in a non-heated garage in the winter. The motor is a bit undersized for the heavy fiberglass boat. With 2 people in the boat it planes out great, with 3 adults or 2 adults and 2 kids it struggles. I have added planing out fins which works great and has helped. We also tried a 4 blade prop with slightly different pitch from the standard 3 blade prop and that has helped. All of these changes have nothing to do with the problem at hand but is just a bit of the history of how we have made a few modifications from the original setup.
We noted early this spring on first trips out on the water that it was act like it was running out of fuel at higher rpms. This was not going into limp mode but just bogging down and completely quitting when running at high rpms. Stop, pump the bulb a little and it started right back up. We had to run on idle back to the dock a few times as it seemed to only get a small supply of fuel at a time and could only run at idle.
Started tearing into the fuel system....
Replaced low pressure filter, high pressure filter (both seemed unplugged), low pressure fuel pump (didn't know how to test this) and the fuel water separator filter. The fuel water separator actually was quite clean but quite old so just did it as a 'good measure'. When we retested we had no change in our problems. We then inspected plugs (slight signs of wear and easy to replace so we did) and inspected fuel injectors. The bottom of the 3 injectors had sticky ethanol deposits and the O ring between metal threads and the injector (cushion) broke in half as it was removed. Replaced 3 injectors although they tested good on ohm test figured it was the 15 year maintenance time anyway. Bummed that injectors don't ship with the bottommost O-ring or cushion and had to order those separately. Got that all fixed, still no joy.
Removed manifold and inspected high pressure pump and checked the filter on the bottom of the pump and the fuel expansion housing for crud. Float was good, chamber was pretty clean and old pump looked pretty good though stained. Still changed pump and cleaned everything just because I didn't want to tear manifold back off again.
All filters and pumps changed still no good. Then started swapping tanks (we use an external plastic 6 gallon tank since we don't go far) no change so blockage wasn't in the tank or the tank fuel barb. Swapped fuel line connector clip on ends, no change. Then took off the access cover to the electrical lines and fuel lines that go down the center of the floor of the boat and pulled out all the tubing, undid zip ties going under the back live well and to the motor and found someone had put an inline brass barb splice in the fuel line near the rear. It was never visible unless you removed all the hose. Removed the splice and tested the various segments of fuel line that we had uncovered and found one was plugged, probably the one right downstream from the barb splice!!
I was feeling good about finding the problem!! I relocated the fuel/water separator to under the rear seat so that the hoses going from the plastic fuel tank to the filter and then to the motor were much shorter than having the lines go all the way to the center console and back like they did before. With clear lines, new filters, new pumps, spark plugs and fuel injectors we had to be all set and smooth motoring in the future right!
In the process of removing things the idle speed thingy that threads in and out and controls engine idle was removed. I don't know exactly how to set that back to the proper setting. I tried a few settings till it ran on muffs at a nice low idle. Certainly on muffs it ran better at higher rpms now but it seemed like no matter what we did we could not get it to idle well. It now had a NEW shake at low rpms and would not run smoothly.
Took it out on the water and it started a little hard and would shake and run like it was running lean or running on 2 of 3 cylinders at low rpms. Once we gave a little rpms beyond 2000 it evened out and ran great. At high rpms it is smooth as ever so can't imagine a cylinder miss. I found the idle set point on muffs was OK but when running it in water it needed a little higher idle to keep it from shaking and stalling. Turned idle speed thingy in slightly till a little higher idle was achieved. Still didn't fix the rough run condition at low rpms
We have no engine light and I don't believe any past codes either.
All the boat shops are on 3 week wait time due to COVID and lack of parts. We are going on vacation and REALLY want to get this fixed.
I've read about gunk in the cooling system on this forum so I took thermostat out, no gunk, tested it in a pan and it opened between 140 and 150 deg F (60-70C)
Last night I dropped the foot and inspected the water pump system. It did seem to me that pressure of the water stream out the tell tale was a bit weaker when we last used it and maybe even a bit intermittent in the stream when watching it this spring. We had no evidence of overheat. The rubber impeller was not damaged and ends seemed to look OK, but the rubber was stiff and pretty much stuck in the swept back position. Housing was in great shape not warped or cracked. I saw a little bit of rubber stain on one side of the housing so maybe the rubber did get hot at one point? I cleaned housing with a little steel wool, replaced gasket, metal wear plate and impeller and added a little silicone grease. While foot was off I inspected the poppet valve which I could only see but not get at. It was closed, no debris, nothing stuck in the opening like others found.
I was considering filling the thermostat housing and water system from the top down with strong vinegar solution as I don't have a barrel big enough to do a vinegar circulation but I can't say that will help since we don't have a overheat condition. This motor was never in salt water and I see no corrosion in the water lines.
Bottom end gears? Seem to shift between gears fine, I changed lower end oil last fall at winterize time and looked good only a hint of milky white, rechecked oil level now and oil is still clean and full. Motor is always trailer transported to and from a boating event and never sits parked in the water.
I have no access to suzuki diagnostics but with no code would that even help?
What makes a the engine shake at idle and then smooth out at about 2000-2500 rpms and run with great smoothness and power at higher rpms? What about changing fuel filters, fuel pumps, spark plugs and injectors with all new parts would make a new problem? Certainly fuel flow should be like new.
It acts as if the engine is trying to compensate from a one time low idle or is getting confused on rich/lean or air/fuel mixture and computer is running it too rich or lean at low rpms.
I read on the forum that an exhaust leak somewhere can do this as well, I can't seem to find any holes and would be shocked that the motor in this good of condition would have a breach somewhere in the metal shell.
I've read the idle air control sensor could be a culprit but would that not throw a code? I can see that sensor and hoses are hooked up and it looks OK but how to test?
If the impeller was the problem and we didn't have good water circulation then I can HOPE that when I get it out on the water again that it might be better but I'm not so confident. One post I read online it was a poor water circulation issue that caused a rough idle or poor engine performance at low RPMS.
IF I need diagnostics I might be able to twist the arm of the local dealer to just scan my outboard codes even though they are swamped with other work.
Thanks for reading this far!
My father in law has a low hour 2005 Suzuki 50hp four stroke mated to a Carolina Skiff. The motor has been a flawless runner. Always started, idled like a dream, ran out at higher rpms with no issues, sipped gas, very fun to run and very quiet for trolling. This boat was used only a few times every summer in freshwater lakes in MI and stored in a non-heated garage in the winter. The motor is a bit undersized for the heavy fiberglass boat. With 2 people in the boat it planes out great, with 3 adults or 2 adults and 2 kids it struggles. I have added planing out fins which works great and has helped. We also tried a 4 blade prop with slightly different pitch from the standard 3 blade prop and that has helped. All of these changes have nothing to do with the problem at hand but is just a bit of the history of how we have made a few modifications from the original setup.
We noted early this spring on first trips out on the water that it was act like it was running out of fuel at higher rpms. This was not going into limp mode but just bogging down and completely quitting when running at high rpms. Stop, pump the bulb a little and it started right back up. We had to run on idle back to the dock a few times as it seemed to only get a small supply of fuel at a time and could only run at idle.
Started tearing into the fuel system....
Replaced low pressure filter, high pressure filter (both seemed unplugged), low pressure fuel pump (didn't know how to test this) and the fuel water separator filter. The fuel water separator actually was quite clean but quite old so just did it as a 'good measure'. When we retested we had no change in our problems. We then inspected plugs (slight signs of wear and easy to replace so we did) and inspected fuel injectors. The bottom of the 3 injectors had sticky ethanol deposits and the O ring between metal threads and the injector (cushion) broke in half as it was removed. Replaced 3 injectors although they tested good on ohm test figured it was the 15 year maintenance time anyway. Bummed that injectors don't ship with the bottommost O-ring or cushion and had to order those separately. Got that all fixed, still no joy.
Removed manifold and inspected high pressure pump and checked the filter on the bottom of the pump and the fuel expansion housing for crud. Float was good, chamber was pretty clean and old pump looked pretty good though stained. Still changed pump and cleaned everything just because I didn't want to tear manifold back off again.
All filters and pumps changed still no good. Then started swapping tanks (we use an external plastic 6 gallon tank since we don't go far) no change so blockage wasn't in the tank or the tank fuel barb. Swapped fuel line connector clip on ends, no change. Then took off the access cover to the electrical lines and fuel lines that go down the center of the floor of the boat and pulled out all the tubing, undid zip ties going under the back live well and to the motor and found someone had put an inline brass barb splice in the fuel line near the rear. It was never visible unless you removed all the hose. Removed the splice and tested the various segments of fuel line that we had uncovered and found one was plugged, probably the one right downstream from the barb splice!!
I was feeling good about finding the problem!! I relocated the fuel/water separator to under the rear seat so that the hoses going from the plastic fuel tank to the filter and then to the motor were much shorter than having the lines go all the way to the center console and back like they did before. With clear lines, new filters, new pumps, spark plugs and fuel injectors we had to be all set and smooth motoring in the future right!
In the process of removing things the idle speed thingy that threads in and out and controls engine idle was removed. I don't know exactly how to set that back to the proper setting. I tried a few settings till it ran on muffs at a nice low idle. Certainly on muffs it ran better at higher rpms now but it seemed like no matter what we did we could not get it to idle well. It now had a NEW shake at low rpms and would not run smoothly.
Took it out on the water and it started a little hard and would shake and run like it was running lean or running on 2 of 3 cylinders at low rpms. Once we gave a little rpms beyond 2000 it evened out and ran great. At high rpms it is smooth as ever so can't imagine a cylinder miss. I found the idle set point on muffs was OK but when running it in water it needed a little higher idle to keep it from shaking and stalling. Turned idle speed thingy in slightly till a little higher idle was achieved. Still didn't fix the rough run condition at low rpms
We have no engine light and I don't believe any past codes either.
All the boat shops are on 3 week wait time due to COVID and lack of parts. We are going on vacation and REALLY want to get this fixed.
I've read about gunk in the cooling system on this forum so I took thermostat out, no gunk, tested it in a pan and it opened between 140 and 150 deg F (60-70C)
Last night I dropped the foot and inspected the water pump system. It did seem to me that pressure of the water stream out the tell tale was a bit weaker when we last used it and maybe even a bit intermittent in the stream when watching it this spring. We had no evidence of overheat. The rubber impeller was not damaged and ends seemed to look OK, but the rubber was stiff and pretty much stuck in the swept back position. Housing was in great shape not warped or cracked. I saw a little bit of rubber stain on one side of the housing so maybe the rubber did get hot at one point? I cleaned housing with a little steel wool, replaced gasket, metal wear plate and impeller and added a little silicone grease. While foot was off I inspected the poppet valve which I could only see but not get at. It was closed, no debris, nothing stuck in the opening like others found.
I was considering filling the thermostat housing and water system from the top down with strong vinegar solution as I don't have a barrel big enough to do a vinegar circulation but I can't say that will help since we don't have a overheat condition. This motor was never in salt water and I see no corrosion in the water lines.
Bottom end gears? Seem to shift between gears fine, I changed lower end oil last fall at winterize time and looked good only a hint of milky white, rechecked oil level now and oil is still clean and full. Motor is always trailer transported to and from a boating event and never sits parked in the water.
I have no access to suzuki diagnostics but with no code would that even help?
What makes a the engine shake at idle and then smooth out at about 2000-2500 rpms and run with great smoothness and power at higher rpms? What about changing fuel filters, fuel pumps, spark plugs and injectors with all new parts would make a new problem? Certainly fuel flow should be like new.
It acts as if the engine is trying to compensate from a one time low idle or is getting confused on rich/lean or air/fuel mixture and computer is running it too rich or lean at low rpms.
I read on the forum that an exhaust leak somewhere can do this as well, I can't seem to find any holes and would be shocked that the motor in this good of condition would have a breach somewhere in the metal shell.
I've read the idle air control sensor could be a culprit but would that not throw a code? I can see that sensor and hoses are hooked up and it looks OK but how to test?
If the impeller was the problem and we didn't have good water circulation then I can HOPE that when I get it out on the water again that it might be better but I'm not so confident. One post I read online it was a poor water circulation issue that caused a rough idle or poor engine performance at low RPMS.
IF I need diagnostics I might be able to twist the arm of the local dealer to just scan my outboard codes even though they are swamped with other work.
Thanks for reading this far!
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