Hello,
I have a 91 dt 140 suzuki oil injected and it is carburated. With 340hrs on it & it is very clean well taken care of. I purchased this spring from a friend that's father passed away. Her father purchased new & took extremely good care of it. Boat was fogged for winter but sat for approx. 3-4 years before she sold to me. He had professionally serviced regularly.
It starts & idles fine but when out on lake hit throttle & bogs out under load? I ran entire day at low rpms tugging around runs fine, but as soon as hit for higher rpms it just blaaa & won't plane out . Sometimes it seems to surge slightly up then down, if I hit waves it sometimes surges down, but most of the time it won't get past 2500-3000 mark. Like it's dropping a cylinder then picking it up quick then in & out. No alarms going off? It sometimes comes out of it & gets full rpm until I slow it down again then tends to go back into this. Does have a crack on the bracket that holds the choke solenoid not sure that this would effect anything? I would think that only on the starting end of things.
I replaced gas hose, bulb water separator filter twice, didn't see water in gas when dumped water seperator filter Gas into a jar, put a new fuel filter strainer kit in it, changed oil injection oil out, new gas, sea foam...has good compression had a shop put carb kits in, fuel pump diaphragm kit, they also did a leak down test & said motor was. Like new yet. They also said it is flooding 3 & 4 cyl but has good spark. They are lost.
I have had to 2 shops & all I get is we can't figure it out motor is like new? do you want a new motor? This Is not an option. Seems they don't want to deal with older suzuki. I thought suzuki dealer dealt in everything not just new motors? I am extremely frustrated & love this boat but I may have to put up for sale if can't get someone in area that knows anything on these. Getting deep in dead end trouble shooting costs.
Note the day I put fuel pump diaphragm kit in it did run very well for about 2hours? Not sure if that was by coincidence? Went back to running poor soon after.
Thank you all for the help.
I have a 91 dt 140 suzuki oil injected and it is carburated. With 340hrs on it & it is very clean well taken care of. I purchased this spring from a friend that's father passed away. Her father purchased new & took extremely good care of it. Boat was fogged for winter but sat for approx. 3-4 years before she sold to me. He had professionally serviced regularly.
It starts & idles fine but when out on lake hit throttle & bogs out under load? I ran entire day at low rpms tugging around runs fine, but as soon as hit for higher rpms it just blaaa & won't plane out . Sometimes it seems to surge slightly up then down, if I hit waves it sometimes surges down, but most of the time it won't get past 2500-3000 mark. Like it's dropping a cylinder then picking it up quick then in & out. No alarms going off? It sometimes comes out of it & gets full rpm until I slow it down again then tends to go back into this. Does have a crack on the bracket that holds the choke solenoid not sure that this would effect anything? I would think that only on the starting end of things.
I replaced gas hose, bulb water separator filter twice, didn't see water in gas when dumped water seperator filter Gas into a jar, put a new fuel filter strainer kit in it, changed oil injection oil out, new gas, sea foam...has good compression had a shop put carb kits in, fuel pump diaphragm kit, they also did a leak down test & said motor was. Like new yet. They also said it is flooding 3 & 4 cyl but has good spark. They are lost.
I have had to 2 shops & all I get is we can't figure it out motor is like new? do you want a new motor? This Is not an option. Seems they don't want to deal with older suzuki. I thought suzuki dealer dealt in everything not just new motors? I am extremely frustrated & love this boat but I may have to put up for sale if can't get someone in area that knows anything on these. Getting deep in dead end trouble shooting costs.
Note the day I put fuel pump diaphragm kit in it did run very well for about 2hours? Not sure if that was by coincidence? Went back to running poor soon after.
Thank you all for the help.
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