Hi folks. I am new on here. Just bought a brand new DF 2.5s for my inflatable Sea Eagle SE9 for fishing. I've used it three times. The first two times I took it real easy for the break in, mostly idling, trolling and running at low throttle. It works alright, but pushing an inflatable through the water is like pushing a mattress. Here are my observations and questions so far. Sorry for the long post. Any help would be appreciated.
- First time out, it ran like a dream. Started on second pull. I never opened up the throttle, and ran it about five hours. Second time out I opened up the throttle a bit more, but immediately noticed an issue. Even after what I thought was ample idling time for the engine to get warm, opening the throttle at all while in gear would cause the motor to stall. I could usually save it by quickly dethrottling back to idle, but it was very difficult to get the rpms up while in gear. Only by babying it repeatedly could I get it to rev up. Once I did, after running for a while in gear, it seemed to work a lot better. Question: is this a) normal, in the sense that it just takes a long time to get this engine warmed up?, b) a clogged jet (already?), or c) bad gas (I tried a different brand of gas, 93 octane, and added some Sea Foam, but it hasn't made any difference)?
- I bought this motor because I was told by a Sea Eagle rep that 2.5 hp would be adequate, I read good things about it, I could afford it, and it is super light (30 lbs.). The max the boat will take is 4hp, and because it has a displacement hull, it's going to go the same speed (5 mph max) no matter the size of the motor. It is still much faster than the trolling motor I was using previously. Still, I worry that I might damage the motor because of the strain of pushing an inflatable. Is that a legitimate concern? It actually seems to push the Sea Eagle better with someone sitting in the front, as opposed to just me in the back. Judging the propeller depth is difficult. With no one on the boat, the cavitation plate is right at the surface of the water. But when I put my 210 lbs. on the rear seat it drops four or five inches under water. I think this may be adding to the strain, so I am going to try raising the transom a couple of inches to see if that helps smooth things out.
- This morning I hooked the motor to a trash can and started it. I noticed no water coming out of the pee hole, so I immediately shut it off. Everything looked normal on the lower unit, so I unscrewed the pee hole plug and found a tiny piece of what appeared to be black plastic debris (about half the size of a grain of rice) blocking the hole. After I replaced the plug and started the engine, everything worked fine. Questions: How did this debris get in the pee hole? Isn't there a screen on the impeller that is supposed to keep this stuff out? My concern is that it could it have come from somewhere internal, i.e., something broken. Any thoughts on this? I used the boat all day yesterday, but never noticed any issue. The water discharge was working fine, but I don't think I looked at it during my last run back to the boat dock where I ran it full throttle for probably 15 minutes. If it was blocked during that time, could I have done some damage through overheating? If so, would that be apparent? It seems to be working fine right now.
Thanks in advance for any input on these issues.
- First time out, it ran like a dream. Started on second pull. I never opened up the throttle, and ran it about five hours. Second time out I opened up the throttle a bit more, but immediately noticed an issue. Even after what I thought was ample idling time for the engine to get warm, opening the throttle at all while in gear would cause the motor to stall. I could usually save it by quickly dethrottling back to idle, but it was very difficult to get the rpms up while in gear. Only by babying it repeatedly could I get it to rev up. Once I did, after running for a while in gear, it seemed to work a lot better. Question: is this a) normal, in the sense that it just takes a long time to get this engine warmed up?, b) a clogged jet (already?), or c) bad gas (I tried a different brand of gas, 93 octane, and added some Sea Foam, but it hasn't made any difference)?
- I bought this motor because I was told by a Sea Eagle rep that 2.5 hp would be adequate, I read good things about it, I could afford it, and it is super light (30 lbs.). The max the boat will take is 4hp, and because it has a displacement hull, it's going to go the same speed (5 mph max) no matter the size of the motor. It is still much faster than the trolling motor I was using previously. Still, I worry that I might damage the motor because of the strain of pushing an inflatable. Is that a legitimate concern? It actually seems to push the Sea Eagle better with someone sitting in the front, as opposed to just me in the back. Judging the propeller depth is difficult. With no one on the boat, the cavitation plate is right at the surface of the water. But when I put my 210 lbs. on the rear seat it drops four or five inches under water. I think this may be adding to the strain, so I am going to try raising the transom a couple of inches to see if that helps smooth things out.
- This morning I hooked the motor to a trash can and started it. I noticed no water coming out of the pee hole, so I immediately shut it off. Everything looked normal on the lower unit, so I unscrewed the pee hole plug and found a tiny piece of what appeared to be black plastic debris (about half the size of a grain of rice) blocking the hole. After I replaced the plug and started the engine, everything worked fine. Questions: How did this debris get in the pee hole? Isn't there a screen on the impeller that is supposed to keep this stuff out? My concern is that it could it have come from somewhere internal, i.e., something broken. Any thoughts on this? I used the boat all day yesterday, but never noticed any issue. The water discharge was working fine, but I don't think I looked at it during my last run back to the boat dock where I ran it full throttle for probably 15 minutes. If it was blocked during that time, could I have done some damage through overheating? If so, would that be apparent? It seems to be working fine right now.
Thanks in advance for any input on these issues.
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